Project/Area Number |
22560804
|
Research Category |
Grant-in-Aid for Scientific Research (C)
|
Allocation Type | Single-year Grants |
Section | 一般 |
Research Field |
Earth system and resources enginnering
|
Research Institution | Hokkaido University |
Principal Investigator |
FUJII Yoshiaki 北海道大学, 大学院・工学研究院, 教授 (70192309)
|
Co-Investigator(Kenkyū-buntansha) |
KODAMA Jun-ichi 北海道大学, 大学院・工学研究院, 准教授 (70241411)
|
Project Period (FY) |
2010 – 2012
|
Project Status |
Completed (Fiscal Year 2012)
|
Budget Amount *help |
¥3,770,000 (Direct Cost: ¥2,900,000、Indirect Cost: ¥870,000)
Fiscal Year 2012: ¥650,000 (Direct Cost: ¥500,000、Indirect Cost: ¥150,000)
Fiscal Year 2011: ¥780,000 (Direct Cost: ¥600,000、Indirect Cost: ¥180,000)
Fiscal Year 2010: ¥2,340,000 (Direct Cost: ¥1,800,000、Indirect Cost: ¥540,000)
|
Keywords | 岩石 / 変形 / 破壊 / 浸透率 / 封圧 / 温度 / 支笏溶結凝灰岩 / 圧縮 / 排水等方圧密試験 / 透水係数 / 排水三軸圧縮試験 / 研磨薄片 / ひずみ硬化 / エンドキャップ / ポアの圧壊 |
Research Abstract |
Triaxial compression tests were carried out on Shikotsu welded tuff,Kimachi sandstone and Inada granite under several confining pressures and temperatures,aiming to clarify permeability variation and mechanisms of it. It was clarified thatpermeability decreased by failure for tuff and sandstone and that flow rate increased underhigh temperature. It would be expected that these findings will contribute for design andconstruction of safer underground openings with lower cost.
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