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2014 Fiscal Year Final Research Report

Study on performance improvement of a microwave discharge ion engine by dynamic control of internal plasma

Research Project

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Project/Area Number 23560962
Research Category

Grant-in-Aid for Scientific Research (C)

Allocation TypeMulti-year Fund
Section一般
Research Field Aerospace engineering
Research InstitutionNishinippon Institute of Technology

Principal Investigator

TAKAO Yoshiyuki  西日本工業大学, 工学部, 教授 (60206711)

Project Period (FY) 2011-04-28 – 2015-03-31
Keywords推進・エンジン / 航空宇宙工学 / ロケット / 宇宙推進 / イオンエンジン / マイクロ波放電
Outline of Final Research Achievements

In this study, a microwave discharge ion engine (5cm in diameter) with variable magnetic field was fabricated and its performance tests were carried out. A movement mechanism of the movable magnets and the control circuit of the mechanism to change the internal magnetic field of the ion engine were developed to construct the ion engine. On the experimental parameters of Xe gas flow rate, movable magnet position and input microwave power, the performance tests were carried out using two kinds of grids made of fine carbon or molybdenum and were different in opening ratio. In these performance tests, the plasma ignition performance of the ion engine was remarkably improved by changing the background magnetic field with the movable magnet. Furthermore, the change of the inner plasma shape of the ion engine and extracted ion beam current from it were observed.

Free Research Field

プラズマ工学

URL: 

Published: 2016-06-03  

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