Long-term behavior of joint connection in steel-concrete hybrid structural system
Project/Area Number |
15H04030
|
Research Category |
Grant-in-Aid for Scientific Research (B)
|
Allocation Type | Single-year Grants |
Section | 一般 |
Research Field |
Structural engineering/Earthquake engineering/Maintenance management engineering
|
Research Institution | Saitama University |
Principal Investigator |
Maki Takeshi 埼玉大学, 理工学研究科, 准教授 (60292645)
|
Co-Investigator(Kenkyū-buntansha) |
斉藤 成彦 山梨大学, 大学院総合研究部, 教授 (00324179)
浅本 晋吾 埼玉大学, 理工学研究科, 准教授 (50436333)
|
Project Period (FY) |
2015-04-01 – 2018-03-31
|
Project Status |
Completed (Fiscal Year 2017)
|
Budget Amount *help |
¥18,460,000 (Direct Cost: ¥14,200,000、Indirect Cost: ¥4,260,000)
Fiscal Year 2017: ¥1,690,000 (Direct Cost: ¥1,300,000、Indirect Cost: ¥390,000)
Fiscal Year 2016: ¥5,330,000 (Direct Cost: ¥4,100,000、Indirect Cost: ¥1,230,000)
Fiscal Year 2015: ¥11,440,000 (Direct Cost: ¥8,800,000、Indirect Cost: ¥2,640,000)
|
Keywords | 鋼-コンクリート複合構造 / 直列混合桁 / 接合部 / 長期変形 / ずれ止め / 押抜き試験 / クリープ / 混合構造接合部 / 長期性能 / 疲労 / 長期挙動 |
Outline of Final Research Achievements |
The long-term external load acting on steel-concrete joint connection in steel-concrete hybrid structural system may induce additional deformation in shear connectors and their surrounding concrete. The long-term slip increment in shear connecting system leading to the deformation of joint connection is experimentally and numerically clarified in this research. The push-out test specimens with headed stud shear connectors were loaded with sustained external shear force for a month, and the long-term slip was numerically simulated by nonlinear finite element analysis. Furthermore, the long-term sustained loading test of joint connection between composite girder and prestressed concrete girder was also conducted so that the long-term deflection increment under various load level was quantified.
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Report
(4 results)
Research Products
(2 results)